OK Here is the final diagnosis on the mysterious shifting issue that has had Aric chasing it for some time now. He data logged the crap out of the car, and has concluded the tune is fine. He made some minor tweeks, but the problem actually lies with not being able to hook the tires.
He has in one log, where he launched the car with violent spin, that commanded shifting early, and when it finally hooks, it commands a downshift because of slower wheel speed - like it should. He kept the logger going and brought the car to a stop and launched it again, only this time, it hooked. Bam, bam, bam, and the car went through the gears perfect. He was able to duplicate this test a couple times, and is convinced the tune is doing what it was designed to do.
The new front tires that now matched the circumference of the rear drag radials, fixed the bouncing speedo needle, and the stock 327 speedo gear is back in the car.
I should pick up the car tomorrow or Saturday, whenever he has JC detail it for me.
Now the big test will be when I take the car to the track, whenever this daggum rain stays away for a weekend.
I finally had Ryan print off a copy of The Marks final dyno sheet, with the new T-Trim and 3.33 pulley. This is with the neutered street tune and big pulley that I asked them to do, to keep it way way safe. This is the tune that is in the car now. One of the nicest graphs I have seen with 0 smoothing. Aric is my hero...