96_Lincoln_LSC
Dedicated LVC Member
Well, Spent Thursday night replacing the power brake booster, Spent Friday letting my back recover... Spent Saturday replacing the Drivers side seat track only to find the plastic base for drivers seat cracked in half too... FUBAR! anyway went and braced the plastic in several differnt locations.. now stronger then original... yea! after the slice and dice on my hands and arms from thursday and Saturdays events, I then had to replace the Air Ride compressor and Fuel filter since I was in there any way, also remove the air silencer cone from under the Filter box, Car seems a bit more peppy!
Side note, the compressor is working fine, however the original issue is not resolved! The car pumps up fine and will inflate the bags in less the 30 Seconds, only after I take it on a ride that causes the system to auto lower at speed, I get the check air message, could this be the "SS Relay"?
What doi you all think. Is this a possible symptom? could replacing the relay solve this? I do just happen to have a spare but really didnt want to rip it apart again.. Oh I did hear the Compressor (originally) surge, surge, surge momentary prior to replacing it.. like it would engage for a second, then cut out.. I thought it was the electric motor binding when it got too hot.. that is what it seems like to me. could it just have been the relay crapping out?
Side note, the compressor is working fine, however the original issue is not resolved! The car pumps up fine and will inflate the bags in less the 30 Seconds, only after I take it on a ride that causes the system to auto lower at speed, I get the check air message, could this be the "SS Relay"?
What doi you all think. Is this a possible symptom? could replacing the relay solve this? I do just happen to have a spare but really didnt want to rip it apart again.. Oh I did hear the Compressor (originally) surge, surge, surge momentary prior to replacing it.. like it would engage for a second, then cut out.. I thought it was the electric motor binding when it got too hot.. that is what it seems like to me. could it just have been the relay crapping out?