While driving last night the car suddenly began misfiring pretty severely. I don't have any explanation why.
The IMRCs on the car have been leaking some air, but this hasn't caused any symptom this severe to date. Could the o-ring have failed so suddenly and dramatically and cause this.
Other than that, I'm stumped. I just put the Actron scanner on the car and pulled no codes other the:
538- Insufficient RPM change during Dynamic Response Test
(Engine Run Self-Test).
632- Overdrive Cancel Switch(OCS) –
no switch action detected during Engine Run Self-Test.
I just refilled the gas tank with 93 Premium and added a bottle of anti-freeze in case bad watery gas was the cause. This failed to solve the problem.
Any ideas?
The IMRCs on the car have been leaking some air, but this hasn't caused any symptom this severe to date. Could the o-ring have failed so suddenly and dramatically and cause this.
Other than that, I'm stumped. I just put the Actron scanner on the car and pulled no codes other the:
538- Insufficient RPM change during Dynamic Response Test
(Engine Run Self-Test).
632- Overdrive Cancel Switch(OCS) –
no switch action detected during Engine Run Self-Test.
I just refilled the gas tank with 93 Premium and added a bottle of anti-freeze in case bad watery gas was the cause. This failed to solve the problem.
Any ideas?